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主办单位:煤炭科学研究总院有限公司、中国煤炭学会学术期刊工作委员会
韩城煤层气田煤层气井排采精细控制模式研究
  • Title

    Study on fine control mode of gas drainage from coalbed methane wells in Hancheng Coalbed Methane Field

  • 作者

    毛得雷康永尚李树新王会娟闫霞李永洲

  • Author

    MAO Delei,KANG Yongshang,LI Shuxin,WANG Huijuan,YAN Xia,LI Yongzhou

  • 单位

    煤层气开发利用国家工程研究中心中联煤层气国家工程研究中心有限责任公司中国石油大学(北京)地球科学学院中国石油大学(北京)油气资源与探测国家重点实验室中石油煤层气有限责任公司临汾分公司

  • Organization
    1.National Engineering Research Center of Coalbed Methane Development and Utilization,Beijing ,China;2.National Engineering Research Center of China United Coalbed Methane,Beijing ,China;3.School of Geosciences,China University of Petroleum(Beijing),Beijing ,China;4.State Key Lab of Petroleum Resources and Prospecting(Beijing),Beijing ,China;5.Linfen Branch,PetroChina Coalbed Methane Company Limited,Linfen ,China
  • 摘要

    为了完善煤层气井排采模式,通过在韩城煤层气田长期的现场排采实践,在现有“两期、五阶段”煤层气井阶段排采模式的基础上,从煤储层解吸-扩散-渗流的角度分析,认为憋压排水-产能释放阶段出现套压和动液面快速波动的现象,是由于现行排采制度与高煤阶、低渗透煤储层的供流能力不完全匹配引起的。依据稳定控制井底流压压降和排采工作制度与地层供流能力相适应的基本思想,将现场采用的模式进行了修正和完善,提出了“两期、六阶段”煤层气井排采精细控制模式,现场试验表明,按照这一精细控制模式,可避免出现套压和动液面快速波动的现象,降低出砂事故率。

  • Abstract
    In order to improve the gas drainage mode of the coalbed methane well,with a long term site gas drainage practices in Hancheng Coalbed Methane Field,based on the sectional gas drainage mode of the available “two periods and five stages” coalbed methane well,from a view of the desorption-diffusion-seepage of the coal reservoir,the analysis held that at the stage of the pressure built-up water drainage-the production capacity released,the rapid fluctuation phenomenon of the casing pressure and dynamic fluid level occurred were caused by the uncompleted matching of the flow supply capability due to the present gas drainage system with the high rank coal and low permeability coal reservoir.According to the stable control of the pressure drop of the flow pressure at the bottom of the well and the gas drainage working system with a basic idea relative suitable to the flow supply capacity of the strata,a modification and improvement was conducted to the site applied mode and a gas drainage fine control mode of the coalbed methane well with “two periods and six stages” was provided.The site test showed that according to the fine control mode,the rapid fluctuation wave phenomenon of the casing pressure and dynamic flow level could be eliminated and the sand flow accident ratio could be reduced.
  • 关键词

    韩城煤层气田低渗透高煤阶储层煤层气井排采工作制度扩散-渗流机理精细控制模式

  • KeyWords

    Hancheng Coalbed Methane Field; low permeability and high rank coal reservoir; coalbed methane wells; gas drainage working system; diffusion-seepage mechanism; fine control mode

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